At the end of last year, Wensheng Glass Co., Ltd. invested 17.5 million yuan to introduce a 60-square-meter glass tank furnace, which can save energy consumption costs of more than 7 million yuan for the company. According to the person in charge of the company, the previous melting furnaces used small glass tank furnaces of about 40 square meters, which consumed large amounts of energy and did not meet quality standards. After the technological transformation, they adopted a new type of 60 square tank furnace, which greatly increased the melting rate. The consumption of standard coal per ton of glass was more than 100 kilograms more than the original, and the product quality was significantly improved and the output increased by 40%.
Wendeng Wensheng Glass Co., Ltd. actively explores new energy management models, adopts new energy-saving equipment, eliminates outdated production processes and other methods, reduces energy consumption and increases production capacity, and strives to create resource-saving enterprises.
Wensheng Glass Co., Ltd. mainly produces glass bottles and can consume more than 8,900 tons of raw coal each year. It is a big energy consumer. Influenced by the price increase of coal raw materials, the company has established a business strategy of simultaneous development and energy conservation, development and conservation, and has accelerated the elimination of energy-consuming equipment and fully tapped the energy-saving potential. It turned out that their glass tank furnaces are directly coal-fired heating, and the smoke emitted from it causes a lot of pollution to the environment. This article is sourced from China's largest glass bottle trading site Zhonghua Packaging Bottle Network. After heating with a gas furnace, it not only solves the problem. The smoke pollution problem can save 0.8 tons of coal per day. The technicians are currently investing in a new glass melting temperature automation control system with an investment of 300,000 yuan. In the past year, the glass melting process was controlled by the workers based on experience. The temperature parameters fluctuate greatly and the product quality is difficult to control. Qu Huasong, deputy general manager of the company, said that they used a glass tank furnace automation control system. All temperature measurement points were controlled by computers, making the tank furnace relatively stable. Compared with the previous manual control, energy loss was reduced by 10%, and the melting quality was also obvious. Improve the product pass rate by 3%.
It is understood that, since last year, Wendeng Wensheng Glass Co., Ltd. has invested more than 20 million yuan in the introduction of various energy-saving equipment, and companies have thus obtained high returns. In the first half of this year, the company produced more than 30,000 tons of various glass products, an increase of 30% over the same period of last year.

Reprinted Source: China Packaging Bottle Net


Indoor Trampoline Park is becoming more and more popular,it  apply for amusement park,warehouse,shpping mall,indoor theme park,etc.It can be customized according to your location.

1) Indoor Trampoline park plan

plan of indoor trampoline park

2) Indoor trampoline park projects

projects of indoor trampoline park

3) Liben indoor trampoline parks

indoor trampoline park

4) Contact information

contact of indoor trampoline park

Indoor Trampoline Park

Indoor Trampoline Park, Indoor Trampoline Equipment, Indoor Trampoline Park Builder

Liben Group Corporation , https://www.indoortrampoline.de